The Deepwater Horizon Incident: Total lack of any quantitative reasoning initally.
The Deepwater Horizon oil rig explosion and subsequent release of crude oil into the Gulf of Mexico represents a good case study in the lack of using basic scientific principles to make initial, reliable assessments of the amplitude of the problem. More specifically, the overt lack of using quantitative reasoning as part of Federal response policy resulted in paralysis due to initially very low estimates for the volume of crude oil being released. The fact that no one questioned the validity of the initial estimate made only by BP (possibly in some collaboration with the Coast Guard) is a stunning revelation of numerical illiteracy. In the end, the initial estimate will have proven to be incorrect, by a factor of at least 50 (!). Yes, the situation is complicated and somewhat difficult to initially assess and factors of 2-3 uncertainty in complex systems are to be expected; but a factor of 50?-- that usually means fundamental aspects of the problem are just being ignored. While it was in BP's own financial interest to lowball the flow estimates so as to avoid paying substantial fines and penalties, his initial lowballing seemed to dominate the initial view of the problem. Science was nowhere to be found and quantitative reasoning was not initially applied as a means to estimate the flow rate. An apt analogy involves earthquakes: suppose an earthquake occurred in the Los Angeles area at an actual magnitude of 9.0 (devastating-- large scale structural damage) but was reported as being a 7.3 earthquake (50 times less with little structural damage). Clearly, far too little resources would be devoted to the 7.3 perceived event compared to the 9.0 physical reality. In the early days of the Deepwater incident, affairs were strongly driven by perception, driven by a corporate entity (BP), rather than using scientific reasoning to determine the proper reality.
The early estimate of 1,000 barrels per day (bpd)
The Deepwater Horizon explosion occurred on April 20, 2010 which resulted in 11 fatalities and a 2-day fired that destroyed the platform which ultimately sank. Initially, much of the liberated oil was consumed/destroyed by fire. The initial oil slick did not appear until 3 days after the event. The first flow rate estimate of 1,000 bpd was made on April 24 via a joint announcement by the US Coast Guard and BP oil. This number was never put it any context and appears to be nothing more than an arbitrary round number. As a result of this gross underestimate and likely wishful thinking, a "fix it with duct tape" approach seems to have been the initial solution. The amount of needed duct tape is directly related to the size (diameter) of the pipe out of which the oil was flowing and that was either a) unknown at the time or b) information that was not forthcoming from BP. Again, a simple example can help put this in perspective: if you are using your garden hose at full pressure and suddenly that hose is cut in two, the diameter of the leaking hose is the same as the original hose and the water is still gushing out where the hose was severed. Instead, if you drill a 1/4 inch hole in the hose, most of the water will still go through the hose and the leak rate out of the small hole will be much less than the total volume of water flowing through the hose. Indeed, you might even be able to patch that leak with duct tape. This approach adequately describes the initial assessment; 1,000 bpd is sufficiently small to encourage the attempts to simply "patch the hole" and such efforts were made, and of course, they failed. You can't patch the hole in your garden hose if it's been completely severed and essentially, the Deepwater Horizon hose (e.g. the pipe containing the crude oil) was similarly severed.
It is also important to remember three physical parameters of the outflow situation: 1) The source of the outflow is via some severed pipe (called the riser) that is located 5000 feet below water. This means there is a hydraulic head pressure on the top of pipe which would tend to suppress any outflow (and drive ocean water into the pipe) 2) the pipe is fitted with a blowout preventer (BOP) that had a rated pressure of 15,000 psi. The failure of the BOP directly shows that the internal pressure driving the flow could be as high as 15,000 psi, if that pressure can be sustained by the gas/oil pocket that was initially penetrated by the rig; 3) The diameter of the pipe through which the outflow was emanating was initially unknown. This pipe diameter confusion can be seen in Figure 1 where the outflow is coming from some inner diameter core that is embedded in the casing which has a known outside diameter of 21-inches. The pipe in which the flow was emanating is clearly of a smaller diameter and some initial estimates used a value of 9 inches. Note this video image was taken approximately 6 weeks after the initial incident.
Why the flow rate has to be larger than 1000 bpd
The flow rate through any pipe is a function of the internal pressure of the flowing fluid and the diameter of the pipe (as well as the viscosity of the fluid). From these parameters simple physical arguments could have been made at the time showing that the 1000 bpd rate could not possibly be correct. Four such arguments/analogies are given below:
- Bathtub analogy: A household bathtub outflow, as driven by 40 psi water through a 1.5-inch pipe is 5 Gallons per minute (GPM) or the equivalent of 175 barrels per day. Thus 6 household bathtubs would be the equivalent of 1000 barrels a day. Yes, the viscosity of crude oil is higher than water so 2-3 times more bathtubs would be needed but that is still only a handful. This is where the 1000 bpd figure needs to be put in context as nowhere in any media reporting is the simple analogy made with a bathtub that would immediately qualitatively plant seeds of doubt that the flow rate was really this low. In addition, the outflow pipe is much larger than 1.5 and the internal pressure driving the flow is orders of magnitude higher than 40 psi.
- Hydraulic Pressure Argument: A 5000-foot head of water would apply a confining pressure of 7500 psi which would serve to suppress any flow of crude oil out of a pipe. At the time of the accident the deep reservoir pressure in which the rig was drilling was estimated by the Coast Guard to be 8000 psi (by the way, this is the estimate that allowed BP to just use a BOP rated at 15,000 psi). It is this 8000 psi that initially allows the oil to flow vertically up a 4000-meter-long pipe. While in the pipe, the weight of the oil exerts a downward pressure of about 5000 psi. The differential pressure of +3000 psi is what determines the upward crude oil flow rate. If the pipe is severed, the initial pressure of 8000 psi will likely be lower (since now the gas pressure is no longer confined to a pipe). Even if 90% of the original gas pressure (8000 psi) is somehow maintained, that outward pressure is now lower than the confining pressure and the flow is stymied. The fact that it was not stymied is a strong indication that the internal pressure which was tapped was significantly larger than 8000 psi and this served to cause the BOP failure that triggered the surface explosion.
- Real World Example Argument. Mud has similar viscosity to crude oil. Southwest Oilfield products provides specifications for a mud pump rated at 7500 psi (Mud Pump 2017) which produces 300 GPM for a 4.5- inch pipe. This is equivalent to 10,500 bpd, not 1000! At constant pressure, the GPM flow rate will go as the square of the pipe diameter. For an outflow pipe of 9 inches, 10,500 barrels per day expands to 42,000 bpd. For pipe flow, the flow rate goes as the square root of the pressure so if you double the internal pressure to 15,000 psi (because the BOP failed) then the flow rate increases to 1.44 x 42,000 = 60,480 bpd.
- The common-sense argument: Individual oil rigs in the Gulf of Mexico oil fields can have daily production rates as high as 100,000-- 200,000 bpd (e.g. the URSA and Atlantis platforms) with typical averages of 40,000 bpd (BP Working Paper 2010). The Deepwater Horizon did not begin drilling operations until Feb of 2010 so there is no production data on its operations prior to the explosion (it takes a few months for a typical oil rig to ramp up its production). According to the design specs, the Deepwater Horizon platform was capable of producing at least 40,000 bpd which, depending upon the internal pressure supplied by natural gas fields, could go as high as 100,000 bpd. So how is that if you effectively cut the oil pipe in two, the subsequent leakage rate is now only 1,000 bpd?
Thus, simple considerations of likely internal flow pressure and pipe diameter lead to estimates that are at least an order of magnitude larger than 1000 bpd and some estimates made in this manner do come close to the figures determined a full two months later. A "duct tape" solution will clearly not work and this could have been known at the time.
Upwards revision from oil slick image analysis
On April 28, 2010 NOAA scientists "officially" up graded the leak rate to 5,000 bpd. NOAO said this number was uncertain, and of course is still significantly lower than the previous physical reasoning implies. This estimate was largely based on image analysis of the evolving surface oil slick which can be problematical, as discussed below. However, for now we note the following: a) this revised estimate of 5000 bpd will remain the same for approximately a month, b) on May 24, 2010, BP executive Daniel Rainey also provided a 5,000 bpd estimate to Congress, as BP's "best scientific guess" at the flow rate (Rainey would later go on trial for directly lying to congress but was eventually acquitted), c) there is still no video of the leakage that is available for the scientific community to analyze. The first video will not be released until May 12. The NOAA April 28 estimate of the leakage rate is largely based on the following (processed to increase contrast) image of the oil slick as it appeared on April 27:
.For an oil slick to be "visible" from MODIS, its thickness as a floating layer on water must be at least 1 micron. The visible oil slick of April 27 covers 2233 square miles. If the oil slick has a uniform thickness (quite unlikely) of 1 micron then the oil slick would represent
- 5783 cubic meters
- 1,527,705 gallons
- 36,374 barrels.
This visible oil slick did not emerge until April 24 suggesting that the leaking oil had been initially consumed by the 2-3 day fire that occurred before the rig sank. For an oil slick to grow to this volume in 3 days implies a leakage rate of ~ 12,000 bpd. Also, at this time a BP exec claimed that 3% of the slick was 100 microns thick and the remaining 97% was "only one or two molecules thick". Well, that's a physically absurd statement to make. Oil slicks are diffusive and tend toward uniform thicknesses except when interrupted by coastlines where the oil piles up. In addition, a one or two molecule "thick" oil sheen will not return any spectral signature back to the satellite to even be detected. If we take BP at their word on the 3% value of 100 microns and the rest at least at one micron (to ensure there is a detection of the slick), then the resulting volume is now 4 times higher at 6 million gallons or a flow rate of 40,000 bpd. The thickness of the oil is the critical factor for using image analysis of oil spills to determine the flow rate and it takes many days of images to best estimate this. Hence the NOAA estimate of 5000 bpd really is premature and could easily be an underestimate. Still this revision is qualitatively important as it means the "disaster is larger than we initially thought". This important sentiment was proposed in various blogs and other social media forums at the time.
Quantitative analysis of in situ video data.
We are now a week into the crises and most of this time has been spent trying to "cap" the flow and to start surface clean up efforts. All the time, the oil is gushing out of a pipe of unknown size, under 5000 feet of water, at an unknown flow rate, but a flow rate that is certainly larger than 5000 bpd. Now, for reasons that are rather unclear, it is not until May 12 that video of the flow was publicly released (this is almost 3 weeks after the incident). Immediately after release, many scientists and scientific organizations recognized the real flow rate had to be substantially higher than the 5000 bpd "official rate" just from casual observations of the fluid flow. More precise estimates of the flow rate will be determined by measurements of particle velocity. On May 19 (almost one month since the incident) the Flow Rate Technical Group (FRTG) was formed. This was a group of scientists at various institutes who were given two primary tasks:
- Generate a preliminary estimate of the flow rate as soon as possible
- Within two months generate a final estimate of the flow rate which will be then taken as the official estimate.
Initial estimates by several groups using different methods and techniques range from 24,000 +/- 9000 bpd to 68,000 +/- 14,000 bpd. The range in flow estimates and their uncertainty is largely driven by the variable oil to gas mixture. If this ratio is high, then the combined fluid is more viscous, has larger oil volume but lower particle velocities. If the ratio is low, then the additional gas pressure drives higher flow velocities but gas takes up a larger proportion of the volume. The video data always shows methane bubbles present but the bubbling rate changes; this implies highly variable oil to gas mixture with time so groups that use different time frames of data analysis will get different results, Work documented by the Plume Modeling Team produced a revised estimate on May 27 of 12 -- 19,000 bpd. This was later revised upwards to 25 --30,000 on June 10 and then, in meeting their second charge, the FRTC adopted the range 35,000 to 60,000 bpd.
Could it have been as large as 100,000 bpd?
A video camera will take 24-30 frames per second so the measured flow rates of 1-2 meters per second are easily resolved. Here we show the kind of example calculation that could have been made to illustrate a worst possible case:
- Pipe diameter = 21 inches or a cross section (πr2) = 0.2 square meters (e.g. the entire casing is severed)
- Volume flow rate at 1.0 meter/sec = 0.2 cubic meters per second
- 0.2 cubic meters per second =720,000 liters per hour
- One barrel of oil = 159 liters; 720,000 liters per hour ~ 4500 barrels per hour
- 4500 barrels per hour x 24 hours per day = 108,000 barrels a day
There are two principle uncertainties in going from flow velocity to the final flow rate: a) the determination of the average flow velocity will depend upon the amount of time you include in your analysis so that you can smooth over the large fluctuations to establish a baseline flow velocity. b) in reality there were three separate leaks that were occurring so the combined pipe diameter is difficult to determine. Clearly there is not one main leak occurring at the scale of the 21-inch casing diameter, so the above is an overestimate. At some point in this overall process, an inner diameter of 14 inches was announced and adopting that would decrease the previous estimate by a factor of 2 down to 54,000 bpd.
Overall, because of the presence of gas in the effluent it is scientifically impossible to precisely know the volume flow rate. It is also clear that the actual flow rate could fluctuate considerably from day to day and this fluctuation was plausibly 10,000 to 100,000 bbd. Indeed, internal documents at BP do show
estimates as large as 100,000 bpd were possible . It is also physically likely that the flow rate does start to degrade over time as the internal pressure driving the flow must eventually lower. The final scientific consensus suggests a discharge rate of 50-70,000 bpd yielding an integrated release of 5 million barrels (210 million gallons) into the Gulf of Mexico ecosystem. Sadly, that discharge is actually less than the amount of gasoline used by Americans in a single day.
The principle result from the quantitative view presented here is that the Federal Government in initially dealing with the Deepwater Horizon explosion did not adequately use simple scientific methods to estimate the likely size of the problem. The initial public release statement on the leakage rate will turn out to be 50 times too low. The initial estimate of 1000 bpd has about a 1-week lifetime before it is revised to 5000 bpd -- still a factor of 10 off. It then took another month for an official Federal Task Force flow committee to arrive at a rate of 12,000 --19,000 bpd which is still a factor of 2-3 less than the kind of estimates which could have been made initially. More accurate estimates of the leak rate took about 2 months to generate and established levels of 50 -- 70,000 bpd as the most probable value. By then most of the environmental damage has been done.
We emphasize that these final estimates of the volume leak are close to what could have been estimated on day 1. Indeed, if the size of the spill was initially declared at 50,000 bpd subsequent response to the incident would have been substantially more robust. Instead, a full two months elapsed before this leakage figure would become official. Federal policy needs to be based on having sufficient resources to respond to a worst-case disaster and that response needs to be based on sound, scientific estimates of the amplitude of the event. Federal policy cannot rely on wishful thinking or be controlled by corporate interests, but that is exactly what happened in the case of the Deepwater Horizon oil spill in the initial assessment of the situation
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